DragBikeMike
Serious Thumper
Offline
SuzukiSavage.com Rocks!
Posts: 4411
Honolulu
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At the conclusion of Part 9, we had a 692cc high compression engine. It had a high-flow K&N air filter, high-flow 38mm carb, ported head, DR650 cam, high flow exhaust system, and a lightened flywheel. The Wiseco 97mm flat-top piston increased displacement by 40 ccs, compression by about 3 points (8.5:1 up to 11.4:1) and tightened the quench clearance to .040”. To hold the power, it needed a beefed-up clutch. It ran great. Tons of power, excellent fuel economy, and cooler operating temps. I wanted to put some miles on it before I wrote the final report. So, once the Big Bore Flat-Top had 6200 miles on it, I changed the oil & filter (3rd oil change), checked chain tensioner extension (14.4 mm), adjusted the valves (.007” as-found), cleaned the air filter, checked compression (225 psi) and started writing. But something wasn’t right. After a few miles, the vibration and audible noise seemed higher, the clutch felt like it was slipping, and the oil got black.
When I did the service at 6200 miles, I changed out the oil drain plug. I had been running the old-style non-magnetic plug. I had a newer magnetic drain plug, so I installed it. No particular reason, it just seemed like a good idea. So now I had like 50 miles or so on a fresh oil charge, and the engine was noisy, and things seemed to be shakin more, and the oil was black already. Best take a look.
Oh my! That’s not good.
8/25/23 As it turns out, I believe these chips came from the LH main bearing. At first I suspected the chips were from the failed 5th gear, but later on I discovered that the main bearing had also failed. I simply missed the bearing failure. DBM
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