Hey y'all!
Newish member here from Ottawa, Canada!
I picked up a 93 savage back in September for $1000cad. At the time it ran fine and the only visible issue was the choke popped in as soon as the bike started. PO said he put in a new battery & cleaned the carb. (Mistake #1 was believing him). Past past owner, put on a pod filter, custom highway pegs (pretty sketchy, but fun) and a decent sissy bar. Other wise the bike is stock.
I got just over 100kms of riding in, when my bike started dying at high speeds on decel. Not even thinking it could possibly be the battery (cuz ya know, it was "new"), I had made the assumption my carbs were dirty & probably not jetted for the pod filter. Get the bike home & start investigating- oil smells like gas, battery visibly looks too small, pod filter is attached with plumbing tube. Check PC to see if it's faulty- and it is. Decide my riding season is over & it's a winter project now.
Spent the majority of winter endlessly reading this forum. Thanks so much!!! You have all helped me endlessly! My mechanical skills are minimal at best, but I've been determined to work on my own motorcycles from the start (this will be my 3rd Suzuki, first LS650 & first-time doing all the work myself).
Yesterday was my reassembly day and here's how it went:
I replaced my stock PC with a raptor 660. Ordered jet kit from Lancer & then Pulled the carb, tore it apart completely, switched my jets to 150 & 55 and cleaned everything up real good (I did this 4 times, as I had stripped screws & broken gaskets etc etc). Adjusted my air/fuel mixture screw 1.5 turns out. I left the white spacer washer stock, as I'm not totally sure what that mod is & then I moved the clip up one slot (to the tip of my needle). Capped my vaccum line. Replaced my air pod with an emgo & put on a proper rubber boot instead of the plumbing tube. Changed my oil & filter, spark plug. Bought correct battery for the bike. Reassembled, put new gas in and then crossed my fingers!!!!
The bike started right up!!! Started blowing some smoke so I killed it. Started it again, no problems, no smoke. Idle was lagging so I turned my mixture screw another half turn, and it started to sound really great!!
Heres a YouTube video of how it sounded after a 20min ride. I think I can still adjust my throttle & mixture screw, but otherwise I think I did a good job! Next test will be high speeds & see if it still does on decel, but we're currently being hit with a bunch of rain.
https://youtu.be/pyRqJCwaXcsAdded bonus, popping is minimal compared to when I first bought the bike. Let's out one small "poof" as shut off and I'm cool with that!
My future plans are: changing the bars to ZED Biltwell bars & getting a custom sporty style exhaust made & then I'd like to swap in the Mikuni VM carb by next summer. Hoping to take this bike across Canada & visit some friends in the mountains!
Cheers!!!!